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Legion Of Andromeda

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Everything posted by Legion Of Andromeda

  1. sorry thats my poor terminolgy, i meant the equatorial. ....after sorting out the meshing. it started badly see pic below, but i'm currently getting 0.9 in poor seeing looking east and i havent recalibrated with the lowered the guiding rate yet because there are clouds due south now
  2. sorry, i meant 75 degree altitude, (50 degs in dec) so the scope is nearly vertical for m51 and 101, when i calibrate its usually towards the ecliptic / meridian, ...where do i change the guide correction speed?.... i will swap the camera over.... ive tried longer exposure times to no avail However , since i made this post , i checked the belts which were both tight, but the gear meshing was loose...now waiting for some clear skies to test
  3. I bought a second hand cem40 two months ago in very good condition, aparrently it was checked over / serviced by Altair prior to sale when i first started using it, i was getting 0.8 total RMS, which is fine for a GT81 but it has got steadily worse since then.... between 1.5 and 2 with a random erratic histogram I'm using phd2 dev3 with multistar guiding the scope , mount and tripod is very tight and stable as i can get it No cable drag, all of it is through the mount (2 CABLES) 3d balance is spot on , and the axes are very free-moving i run phd2 calibration every four sessions or so I run the Guiding assistant every time, using its suggestions and i'm using predictive pec algorithm..other algos make little or no difference framerate is anything between 1 and 3 seconds pec playback is 'off' in the mount settings ipolar is bang-on, but goes out very slightly after a slew i dont use my scope if its windy most of my imaging is at 75 degrees +++ lately (maybe thats an issue) my guidescope is WO 50 x 200 and well focused my guide camera is a ZWO mm120 my backlash seems almost non existant, ive set it up during the day and slewed back and forth on a distant object with no delay / backlash....that i can tell of what can i do myself to try / check to improve matters? my CW is towards the end of the bar, do i add another one and shift them both up? whilst i'm reducing inertia, i'm adding mass, so not sure if that helps? is the CEM40 prone to flexure / wobbles? can i improve my backlash? i'm happy to make the necessary adjustments, but lack the documents. is my guidecam / scope any good? what is odd, is that the reported backlash varies tremendously each time i run the Guiding assistant any other ideas would be greatly appreciated
  4. righto, i recently purchased a second hand Ioptron CEM40 mount, it works fine as a standalone mount but has never used in conjunction with the ascom platform. I have experience with ascom in conjunction with ATP and more recently, NINA for connectiing my cameras, focuser and my previous Skywatcher mount However, i hit a brick wall with the cem40. i have a feeling that i need to update the firmware on the mount and the handset,,before setting up the drivers in ascom? any guidance on best practice, cables, additional drivers, pitfalls to avoid, matching software to hardware would be appreciated. The official source of help is a little inconsistant in detail and reliability, so i could do with comments from those that have been down this road and come out the other side Thanks in advance
  5. Under ; Equipment ~ Guider i have PHD2 selected, the others are synchronised PHD2 (experimental), Direct Guider and Lacerta... maybe i should try the experimental option Also,; Options ~Equipment ~ Guider settings. this all looks normal to me with the correct filepath and server port being 4400
  6. i recently migrated from APT to NINA and it's mostly fine except how it relates to phd2. The first two times i fired up NINA it launched phd2 guiding in the first instance, before i had a chance to set up anything else, the trouble with that, is that it grabbed my main camera and allocated it to guiding, not my 120mm So, I switched something off in NINA (cant remember what) which allowed me to install my main camera, focuser and mount...which means i then have to start and run phd manually afterwards, but NINA can't start and stop phd in relation to meridian flips, sequencing, slewing and probably some other stuff. So, how do i get NINA to control phd automatically? am i missing a magic button?
  7. hi there, i have been using PHD2 and APT for nearly 2 years now . i currently have a WO GT81 / ZWO OSC scope on a Skywatcher EQ5 goto mount with a 50mm WO guidescope / ZWO 120mm camera..... All running and guiding very well for a long time with a surprisingly flat histogram for a cheap gear-driven mount via ASCOM on my win10 laptop. However, i recently set up the same softwares and the same PHD2 settings on my PC from inside the house and connected to my rig hub via an active USB cable with no major issues...for a few sessions until last night.... The guiding was very jagged...not drifting off completely, just all over the place.. i restarted EVERYTHING, many times. polar alignment, star alignment, goto was spot-on! plate solving was working etc. So i am going to share my settings to get some feed back to check for any major over-sights or suggestion for improvements. BTW one thing i do remember is that my main scope and guide scope are close but not totally in-line...how important is this?... also, could a flakey serial to usb cable between the handset and the hub affect the commands?.. sorry about no screen shots from the session.
  8. Prior to installing the Arduino, i took a couple of single, unstacked test shots last night using my old D7000 with a 50mm lens, one at 2 mins , the other at 3 mins. Now i have rewired it for the Arduino i can house the electronics in a far smaller box and after that i need to figure out some kind of alt sub-base rather than tilting the top part of my mount
  9. how does this and the sketch you provided earlier apply to my aforementioned setup?. I assumed you had a nema17 hooked up to a Tb6600 (optimised for current and resolution) and an UNO?, plus, your sketch makes no mention of pul, dir and ena which is why i haven't touched it yet. I now have it all running perfectly and quietly in a smaller box than before on a very basic code.
  10. thats an interesting approach to overcoming the tangent error of a straight rod, as long as your coding reflects the maths involved with a rod moving at an increased rate of accelleration to keep the door rotating at a constant rate. The easy driver is nice and compact but i prefer the TB6600 for quick and sturdy connections... adding a reverse switch would be handy for me
  11. ok, I disassembled the old circuit with the variable / manual pulse controller and reassembled with my UNO connected to dir/2 and pul/3 pins and their grounds of course, but no ena? as per most of the sketches and the simplest one not only moved in the right direction but i easily changed the delays from 1000 to 1180 to get the rpm needed for round stars, in this case 0.97 rpm. Apart form your sketch bearing no resemblance to the others, and assuming 13 is pul, i couldn't see any reference to a dir pin. The tb6600 microstep driver has ena, dir and pul
  12. This current post is very different and more specific to my needs and my way of doing research is to collate various sources, including your own, which will all differ in terms of schematics, level of detail, alternative hardware, external links etc ..from which i will form an informed plan with confidence. Most of which has so far referred to the UNO with sketches varying in functionality ...whereas you did say your sketch was intended for the NANO which is probably not an issue, but the concept of using millis is certainly worth investigation.... I have the UNO and 6 sketches including your own but i'm still waiting for the connectors.... early days...the only thing i have done so far is to play with the pin13 LED...I'l let you know how i get on though.
  13. Ok, i have a fairly accurate stepper motor driven barn door tracker. consisting of a NEMA17 stepper motor, a tb6600 driver and a variable pulse generator. I wish to replace the pulse generator with an Arduino uno but i need some guidance and pointers to a schematic and a sketch that works for this setup and only needing to change the speed in the code . the previous post for the finished project here.. thanks in advance
  14. i completely disassembled, gave it a lick of paint and reassembled today
  15. Here she is..... Attention! the images do not correspond directly to the paragraphs, i just put them in to break up the text. - Essentially, it's 2 x birch ply slabs, a control box, hinges, counterweight, mounting plate, tripod ball head, red dot finder, stepper motor, curved threaded brass driver rod . The door and base were going to be in solid oak as i wanted high mass to supress any motor vibrations, but went with 18mm birch ply as it was far easier to machine. I chose stainless steel ball bearing hinges for their smoothness and zero play tolerance, placed as far apart as poss but made sure they were dead inline with each other. i also recessed the hinges into the birch to ensure the inside faces lined up with the hinge pivot point. I then drilled a pilot hole through both boards that was 183mm from the hinge axis and on a centre line for the curved brass rod to pass through. ..The maths is as follows; based on M5 bar giving 0.8mm travel per thread / rotation / 1 minute... therefore 60 mins is 15 degrees of earth rotation and gives 48mm of travel, (15 x 24 = 360 degrees) so; 48mm x 24 = 1152mm circumference / Pi = 366mm diameter = 183mm radius....or if you have no control over the rpms, adjust the values accordingly; faster = larger radius, slower=smaller . It made perfect sense to go with a curved threaded brass rod to ensure a constant rate of rotation and no tangent error. M5 bar gave me sufficient strength but still able to be bent by hand around circular objects of decreasing in size until i got it to retain its diameter when laid over a template. Please note that one should only use the best 30cm from the middle of a 50cm rod. i secured one end to the door using SS wing nuts and washers, the hole needs to be more than 5mm as the rod not only curves through but is angled back so that the working part of the rod starts at a tangent to the inside face of the door and ends up passing through the corresponding hole in the base without to much resistance . I used an existing small Skywatcher dovetail mounting plate which thankfully has a 1/4"-20 threaded hole in the centre to screw onto the top of my existing camera mount, the ballhead is removed and fixed to the door for the camera of course. The mounting plate was offset so the curved rod didn't clash with the tripod pole. The position of the ball head needs to be near the hinge to lessen the weight on the threaded drive nut/rod, but not so close that weight of camera goes past the centre of balance and then pulls on the drive, or worse, the whole assembly flips over and does some serious damage if it goes past that point. . I partially recessed a donated 19mm bearing in the baseboard centred over the drive gear hole. i used a 19mm flat bit for the recess and opened up the hole on the underside to 10mm so that the centre of the bearing could rotate freely and allow the rod to pass without any hindrance. i temporarily added one of the wing nuts to the bottom end of the rod to keep it from flapping around too much whilst i did other things . The gears are at a 1 - 4 ratio. The motor spindle turns a 16 tooth spur gear 4 times for one rotation of the 64 tooth spur gear. The general sizing is in good proportion to the overall kit. In this case i used module1 plastic gears from RS components; 64 teeth with a pitch diameter of 64mm / 8mm bore in conjunction with a 16T/16dia/ 5mm bore... I also bought a spare set of 72 /18 as a back up. I used an M5 insert or 'T' nut fixed to the big gear- not inside the bore as one would think, but inverted so that the threaded shaft of the 'T' nut sits snugly down into the centre of the bearing. I removed the spikes with an angle grinder so that the flange was flat and smooth which i then superglued to the underside of the big gear...getting it central was quite tricky though. I then installed the big gear onto the curved rod most of the way up and it spun pretty well on the bearing and then made finer tweaks to the rod so it stopped touching the bearing but since the gear was very close to the baseboard , i added a small spacing washer which not only lifted it up but got the gear level with the baseboard - which is very important as you want both of the gears to be in line and level with each other. I was tempted to place two insert nuts back-to-back but they would form a straight bore over a curved rod, plus there was a high chance of the two threads binding. . I then installed the NEMA 17 stepper motor. First I transposed the motor dimensions onto the baseboard, I drilled a 25mm clearance hole for the 16T gear, fitted the 16T gear onto the 'D' profile driveshaft but i had to install a small grub screw into the gear hub to hold it in place. i then drilled 4x 4mm countersunk holes for the 25mm machine screws to hold it in place. Its best to slightly oversize these holes if you need to twist it around so the gears mesh nicely. also, if the motor is too low then you can easily raise it up by removing a layer or two of ply from underneath - rather than shifting the gear to the end of the shaft. . Electrics; I fitted an existing decent sized project box to the underside of the baseboard at the hinge end, this contained the speed controller and the stepper motor driver. The input is 12v dc, the 4 motor wires come out of one corner to the motor, i also have a broken + wire from the power socket that goes to a long-armed microswitch, the power is automatically cut when the drive rod gets to certain point for, i hope, obvious reasons. I used an old padlock key clamped between two wing nuts to hit the kill-switch... I'm not going to get into the stepper motor stuff here as it's pretty complex and there are a ton of fantastic tutorials on youtube. . I added a steel counterweight to the other side of the motor...it was needed!.... The ball-head camera mount is attached to a slotted steel plate (butchered from a radiator bracket) with a corresponding 1/4"-20T thumbscrew underneath that sits over a 32mm dia hole in the door, circa 75mm up from the hinge axis . It's very important that the axis of the red dot finder is parallel to the hinge axis. My method was to make a drawing of the section thru the kit that had both axes set out, i then stuck this to a wall 10m away, i used a small laser level against both the x and y axis of the hinge to project that axis onto the drawing in the other room and moved the drawing around until it was correct. i then turned on the red dot finder and adjusted it until the dot lined up with its own position on the section drawing. . I taped over the dials on the red dot finder once i was happy with their position. The proof of the pudding is once you have polar-aligned the tracker, you swing the door between its two furthest points and the red dot shouldn't move relative to the North Celestial Pole. . Speed is of the essence. Mark one of the teeth on the big gear and a corresponding line on the baseboard and using a stopwatch, get as close as you can to 60 seconds for one rotation by altering the dial. then take it outside and set it up, point your camera at something towards the east as this part of the sky moves the fastest relative to us, get your lens focused as best you can, set an exposure of 30 seconds without the motor running and zoom in on the resulting photo and make a note of the trail length, then repeat with the unit turned on...if you're lucky, you will have round stars this time. if not, make tiny adjustments until you do. In my case i ended up with it running slightly slower at 62 seconds on one rotation. . I set my tracker up so that it will do 3 hours / 45 degrees rotation. Any more than that and it will be past it's centre of balance. One could start with the base board angled down from the hinges at 30 degrees to avoid this problem at the end of a long session but i struggled enough with my cheap tripod angling back at 52 degress as it is. i use a basic 1 amp wall transformer at home and a car battery out in the field . The dial controller i have used is a bit of a faff, somewhat hit-and-miss. i might upgrade to Arduino Uno for more precise control when i find the time. but the test results, so far, are very encouraging . I might dismantle and add a lick of paint next weekend. All of the materials / components came to £110. I already had a tripod, small dovetail plate, project box, birch ply, bearing and steel counterweight, .
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